Fixing my FD-6

20 Mar 2016

If you look online you’ll see a lot of complaints about the Roland FD-6 hi-hat pedal getting stiff and being impossible to use. The rubber they use, at least in the version I have, dries out over time and becomes so hard that normal pressure from your foot isn’t enough to move it.

There’s various tricks to fix this, from soaking in hot water to covering with additives to soften the rubber. I tried the boiling method, which worked fine for a couple of months, but after the water escaped it went back to being too stiff to use.

Originally I was tempted to build a replacement board using digital-pots and hall effect sensors but I couldn’t come up with a neat way of adding a battery, charging port and some setup switches to the pedal without cutting it or making it messy.

I've been tempted to try out mold making and casting for a while so I thought this might be a good excuse to give it a go.

The materials

I wanted a replacement for the rubber part, so some form of two part rubber made the most sense. There’s quite a few on the market, but I needed to find something I could get hold of in the UK and I also needed something to make the mold out of.

In the end I used ‘Polycraft GP-3481-F General Purpose RTV Condensation Cure Mold Making Silicone Rubber’ and ‘Polytek Poly PT Flex 60 Liquid Casting Rubber’.

I guessed that the PT Flex 60 would have a similar feel to the original part. 40 sounded a bit too soft and 80 might have been too stiff. At worst, if 60 needed extra strength I could do a second casting with some reinforcing to stiffen it up.

Making the mold

Most of the guides I watched used wooden boxes, usually with a melamine coating then modeling clay along the seams, but I didn’t have any of this handy. As it was a small mold I didn’t think weight would be a problem, so I went with cardboard with a plastic sheet stuck to it to make it water-tight.

Fixing the FD6 - Making the mold

The bits of plastic below the part are some spacers made out of milk bottle to raise it off the base of the mold. I also added two circles of plastic to fill in the hole that’s used to mount it inside the pedal.

Mixing and pouring the mold wasn’t that bad at all. Since you’ve got 30-40 minutes working time there’s no rush and everything I’ve read said that the slower the pour the fewer air bubbles you get.

After casting the mold, and waiting 24 hours to ensure it had set fully, I had this:

Fixing the FD6 - The mold

What isn’t clear from these pictures is that when I was moving the mold I managed to tip the part over. Luckily as the mold was narrow it just ended up at a 30 degree angle, with one corner touching the edge of the mold.

Casting the part

The PT Flex 60 has a pretty short working time (4 minutes) so if any part of this experiment was going to go wrong I assumed it was going to be this.

After a quick 30 second mix I tried my best to pour and get rid of any bubbles. About 3 minutes after mixing it does start to thicken a lot so you need to be well organized.

The data sheet says that it has a two hour curing time, but I left it for 3 just to make sure it was well set before de-molding.

The final part

Fixing the FD6 - The final part

Apart from the corner which touched the edge of the mold it’s a perfect replica of the original, which I don’t think is bad for my first attempt at this.

The data sheet states the it can take up to 7 days for the material to reach it’s specified properties so I’ve placed it over my craft knife, to keep the curved shape, and I’m going to give it a week before I try installing it in my FD-6.

That said, at the moment the stiffness feels about right and while I was worried that it might deform so far there’s no sign of it changing shape at all.

I'll probably get around to doing another quick post saying if it’s working later on.

Future ideas and tips

The mold making process went well but there’s a few things I learned:

Next was casting:

Conclusion

In the end I think it worked pretty well.

My oversized mold cost about £3.70 but I’m sure I could have made it for £2.50 knowing how strong the silicone rubber is now. The final part (all of 27g) was about 62p. Given that the only replacements parts I can find seem to be about £12 on ebay, if you can find them at all, that’s a pretty good price.

Of course, I had to buy a bit more material then I used, but I’m sure I’ll come up with some other interesting things to use it for.